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HomeMy WebLinkAboutAlpha Testing - 8/3/2018 (2)5058 Brush Creek Road Fort Worth, Texas 76119 Geotechnical I Construction Materials I Environmental www.alphatesting.com TBPE Firm No. 813 Our test results and reports are for the exclusive use of the client (and their designated recipients on file in our office) and shall not be reproduced and/or distributed except with express approval of ALPHA. The use of our name and test results must receive our written approval. Test results and reports apply only to the samples tested and/or observed, and are not indicative of the qualities of apparently identical or similar specimens. August 3, 2018 Grapevine - Colleyville ISD 30510 Ira E Woods Ave Grapevine, TX 76051 Attention: Ms. Calva Powell Re: Field Inspection of Structural Steel Mustang Panther Stadium Pkg A & Pkg B Grapevine, Texas ALPHA Report No. F171917-368 Alpha Testing arrived on site to perform a Visual Structural Steel Inspection for the above referenced project. Results of the inspection are as follows: I Beam to beam and beam to column A325 and TCA325 bolted connections – Intermediate level 2 to Press box level 1 – lines 4-1 through E-A and 11-8 through E-A: A. Bolted connections were inspected as per details on S6.3 and S6.4 for lines 4-1 through E-A and 11-8 through E-A. Connections were tensioned to a snug tight condition at time of inspection. Compliant. B. Bolted connections at Press Box level 1 floor framing on sheet S6.4 between lines E-F through 11.1-0.1 and 8-4 through A-F were unable to be inspected due to access. Non-Compliant. II Moment connections – Press box level 1 – Lines 0.13-11.1 and B just past F: A. Welded moment connections were visually inspected as per details on S7.2 welded connections were visually acceptable. As per notes on S7.2 backing bars are to be removed; backing bars have not been removed. Non-Compliant. B. TCA325 bolted moment connections on line B at lines 1 and 11 are snapped and have been completed per details on sheet S7.2. Compliant. III Brace frame welded and A325 bolted connections – Press box level 1 – Lines 0.13-11.1 and B-F: A. Welded connections were inspected per details 1, 2, and 3 on sheet S8.1 and multiple connections were missing welds. Non-Compliant. B. A325 bolted connections were inspected per details on sheet S6.4 and S8.1. Bolted connections were tensioned to a snug tight condition at time of inspection. Compliant. *Discrepancies, if any, are noted above in bold. INSPECTOR: Kevin Ellis CWI#17020871 5058 Brush Creek Road Fort Worth, Texas 76119 Geotechnical I Construction Materials I Environmental www.alphatesting.com TBPE Firm No. 813 Our test results and reports are for the exclusive use of the client (and their designated recipients on file in our office) and shall not be reproduced and/or distributed except with express approval of ALPHA. The use of our name and test results must receive our written approval. Test results and reports apply only to the samples tested and/or observed, and are not indicative of the qualities of apparently identical or similar specimens. ALPHA Report No. F171917-368 We are pleased to be of service on this project and if you have any questions, please contact our office. Sincerely yours, ALPHA TESTING, INC. Tim Begole Sr. Project Manager